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  1. Missed shift 3rd to 2nd with resulting added NVH

    the noise is very possibly wastegate rattle. running VP91 (apparently its more strictly regulated for octane level) supplemented with 1 gallon of VP101. 0 degree knock retard on all cylinders. which at this point is just yet another dataset that suggest zero physical damage to the car. part of...
  2. Engine Noise at ~1500rpm

    yep i have this i recently had a near money shift, just barely below redline. been updating my personal thread on what's been / being done to address/diagnose/fix as needed but yep this noise is exactly what I am experiencing. I'm glad someone was able to capture this via video as i have tried 4...
  3. Missed shift 3rd to 2nd with resulting added NVH

    na bro you're good m8 it's all gravy no hard feelings
  4. Missed shift 3rd to 2nd with resulting added NVH

    update - bottom end is looking good. moving forward with eyeballin the valve train and replacing springs. update to follow
  5. Missed shift 3rd to 2nd with resulting added NVH

    Ive recorded the sound 4 individual times but unfortunately the two phones I have have very poor mic input quality, it's not intelligible from the recordings, you can't really distinguish it. Too much white noise terrible microphones.
  6. Missed shift 3rd to 2nd with resulting added NVH

    Yea I've also been advised that I need to inspect the forced induction side to confirm the turbo bearing. I'm dumping on this thing it'll get back up and running. Sucks but I love the car and I learned my lesson. Will likely end up doing Turbo bearing check Pending result, bore scope to...
  7. Missed shift 3rd to 2nd with resulting added NVH

    yea custom tune was one of the things i was considering, smoother would be better the basemap is a blanket when what i need is a jacket so to speak will have pan dropped and check rod+bearing health within next 1-2 days. result to follow at this point this is for science and my ability to...
  8. Missed shift 3rd to 2nd with resulting added NVH

    Not launching from a dig. Just rolling Motor mounts were checked, they are good torque to spec. I was pistol gripping third to fourth and I was running it hard as hell so I palmed the shifter into second it's clearly user error no debate there dropping pan checking for spun bearing or bent...
  9. Missed shift 3rd to 2nd with resulting added NVH

    violent noise came back yesterday wish i could capture it, my phones have shit audio so i can't despite trying... if i could show you guys a clip you'd understand the concern... the noise at 1600 rpm is voilent
  10. Missed shift 3rd to 2nd with resulting added NVH

    also I did a very correct breakin I've changed oil several times by 5k so when I get the oil reading any lack or presence of solids in the oil based on that will be an indicator clear as day. It's not looking too bad as of now after ongoing monitoring
  11. Missed shift 3rd to 2nd with resulting added NVH

    Have not checked rmm yet it was set at specced 69 lb/ft iirc I'll have to check it. The good news is that I'm still on the next step of oil analysis and this far hVe been unable to recreate the noise issue
  12. Missed shift 3rd to 2nd with resulting added NVH

    update: cylinder 1 - EWMA (weighted moving average) misfire counts - last 10 driving cycles - 4 cylinder 1 - Count for Last/Current driving cycle - misfire counts - 6 cylinder 2 - EWMA (weighted moving average) misfire counts - last 10 driving cycles - 4 cylinder 2 - Count for Last/Current...
  13. Missed shift 3rd to 2nd with resulting added NVH

    it's a good point but all testing is conducted with A/C off. this includes datalogging as a result of extended drive period.
  14. Missed shift 3rd to 2nd with resulting added NVH

    update - ongoing monitoring 1. when cold - not much added NVH beyond added NVH from PRL RMM 2. when hot - after long drives - very much added NVH between 1k - 2k rpms 3. regardless of compression test and leakdown test result being good - i will be doing a check on connecting rods and rod...
  15. Missed shift 3rd to 2nd with resulting added NVH

    results back car in my posession, looks like no damage, may end up doing some motor work anyway this may just be the demark point that begins some motor upgrades anyway like above post stated
  16. Missed shift 3rd to 2nd with resulting added NVH

    my main concern is the notable added noise vibration and harshness between 800-1500 and just about 2100-2300, after the event there is now a noticably louder oscillating vibrational noise that is clearly tied to drive train. anyway i will be recieving results from the compression and leak down...
  17. Missed shift 3rd to 2nd with resulting added NVH

    yea i basically signed up for voided warranty when i ventured into modifying the car, i have made my peace with the void of my warranty, the main problem is the physical damage (if any, hopefully compression test is all good in which case i dust my hands of the issue as well) and getting it...
  18. Missed shift 3rd to 2nd with resulting added NVH

    Fuck man Third gear highway pull, torque steer hit when turbo and VTEC hit pulling my body to the left slightly, just enough to where my hand position when I pulled down to go fourth gear was actually diagonal and therefore put me into second gear at 63 MPH. In theory this speed in second...
  19. 27WON FL5 Exhaust System

    does the downpipe fit under the stock heat shield?
  20. '25 FL5 - Bluetooth audio pop/tick periodically

    Anyone else observing this? Every so often - while playing bluetooth audio (smart phone on youtube music) an audible static pop or tick through the speakers will occur. Usually only happens a single time every so often. driving me nuts. now, I have had aftermarket security installed in the...




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